| 000 | 03167nam a22003257a 4500 | ||
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| 003 | OSt | ||
| 005 | 20260306151646.0 | ||
| 008 | 260306b |||||||| |||| 00| 0 eng d | ||
| 040 |
_aTUPM _bEnglish _cTUPM _dTUPM _erda |
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| 050 |
_aBTH TL 146 _bB47 2025 |
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| 100 |
_aBernardo, Rodel V. _eauthor |
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| 245 |
_aDevelopment of an electric trolley with semi-automated hoist for sedan engine and transmission/ _cRodel V. Bernardo, Miguel Kerby A. Domingo, Rosel Stephen F. Gonzales, Lester Jerota, and David Brian L. Reano.-- |
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| 260 |
_aManila: _bTechnological University of the Philippines, _c2025. |
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| 300 |
_aix, 64pages: _c29cm. |
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| 336 | _2rdacontent | ||
| 337 | _2rdamedia | ||
| 338 | _2rdacarrier | ||
| 500 | _aBachelor's thesis | ||
| 502 |
_aCollege of Industrial Technology.-- _bBachelor of Engineering Technology major in Mechanical Engineering Technology with option in Automotive Technology: _cTechnological University of the Philippines, _d2025 |
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| 504 | _aIncludes bibliographic references and index. | ||
| 520 | _aThis capstone project looked at how small and medium-sized automotive workshops still handle engines and transmissions manually, which can lead to injuries, safety risks, and less efficient work. While there are lifting devices such as hydraulic cranes and automated hoists, many are too costly, too large, or impractical for smaller workshops and teaching labs. This shows there is a need for a more affordable, ergonomic, and semi-automated lifting tool for sedan engines and transmissions. The main goal of this study was to design, build, and test an electric trolley with a semi-automated hoist that can safely lift, rotate, position, and move sedan engines and transmissions. The team used a prototyping approach, which included designing and modeling the system, building it with locally available materials, and running thorough performance tests. The evaluation covered load capacity, ease of movement, rotation accuracy, operation of the electrical and thermal systems, and whether the safety features functioned properly. Tests showed that the prototype could reliably handle up to 150 kg, both with and without a load, without becoming unstable, vibrating too much, or moving unsafely. The system lifted and lowered smoothly, rotated in a controlled way, and was easy to move around in a typical workshop. These results suggest that the new system makes handling engines and transmissions easier and safer. In summary, this project offers a practical, affordable, and ergonomic lifting solution for automotive repair shops and teaching labs, helping to improve safety, efficiency, and hands-on automotive skills. Keywords: electric trolley, semi-automated hoist, engine and transmission handling, automotive ergonomics, material handling systems | ||
| 650 | _aAutomotive technology | ||
| 650 |
_aautomobile engine and transmission _vsedan |
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| 650 | _aElectric trolley | ||
| 700 |
_aDomingo, Miguel Kerby A. _eauthor |
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| 700 |
_aGonzales, Rosel Stephen F. _eauthor |
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| 700 |
_aJerota, Lester _eauthor |
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| 700 |
_aReano, David Brian L. _eauthor |
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| 942 |
_2lcc _cBTH CIT _n0 |
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| 999 |
_c31323 _d31323 |
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